LTC and M1 problem
Posted: Wed Dec 31, 2014 12:57 pm
I have been unable to do a free air calibration with the LTC using the M1 as a gateway device connected via the M1 ethernet.
I am using a M130 with seadoo rxp package and a LTC-NTK (LTC-NTK V1.10C) bitrate 500kbps
In the past I have used a test harness to power the LTC and connect via a UTC-USB to do a free air calibration when replacing a sensor, but I do not have the option to do this if i need to replace a sensor in the field (as happened to me yesterday).
The M1 reads from the LTC, however when I try to do a free air calibration the LTC state remains paused, the sensor will not get hot/warm when i try to do a free air calibration. and the progress bar does not move in the free air calibration window.
Is this a known issue, there has got to be a solution to this problem.
I have tried re-upgrading the LTC firmware, sending the firmware is successful, but it doesnt change anything.
I have had this problem with 3 sea doos already, all exhibit the same behaviour.
I am using a M130 with seadoo rxp package and a LTC-NTK (LTC-NTK V1.10C) bitrate 500kbps
In the past I have used a test harness to power the LTC and connect via a UTC-USB to do a free air calibration when replacing a sensor, but I do not have the option to do this if i need to replace a sensor in the field (as happened to me yesterday).
The M1 reads from the LTC, however when I try to do a free air calibration the LTC state remains paused, the sensor will not get hot/warm when i try to do a free air calibration. and the progress bar does not move in the free air calibration window.
Is this a known issue, there has got to be a solution to this problem.
I have tried re-upgrading the LTC firmware, sending the firmware is successful, but it doesnt change anything.
I have had this problem with 3 sea doos already, all exhibit the same behaviour.